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   rec.crafts.metalworking      Metal working and metallurgy      215,319 messages   

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   Message 213,338 of 215,319   
   Bob La Londe to All   
   I decided to fix it - Sorta Kinda (1/2)   
   19 May 24 17:41:14   
   
   From: none@none.com99   
      
   As I might have mentioned sometime back the Hurco KMB1 has developed   
   backlash and become untunable in the Y axis, and mid job went from   
   tolerable to catastrophic backlash on the X-axis.   
      
   I had decided to scrap it out, and if it had been less work to do so it   
   would probably already be gone.   
      
   The thing is its got the second biggest work envelope of all the mills   
   in the shop, and the biggest of the CNC mills.  Until I bought the South   
   Bend 10x54 knee mill the Hurco was the biggest work envelope mill in the   
   shop.  Its still the heaviest mill at about 4000lbs.   
      
   I am probably going to do something stupid, but I'm doing it anyway.   
   I'm eliminating the servos and putting closed loop steppers on it.   
   Yeah, yeah, yeah...  "Servos rule and steppers drool."  I already have 4   
   absolutely massive Nema 34 closed loop steppers, and one that's even   
   bigger.  They were for another project which I may never get to, and   
   well I can buy more or use the servos on it instead.   
      
   I'm eliminating the belt drive on the Y axis.  I think it may have wound   
   up compounding the backlash on that axis.  It was also sucking up some   
   of the usable power.  It will get a direct drive.  Either a flex plate   
   coupler or a massive helical coupler.  I thought about making it direct   
   drive before, but the servo sticking straight out the front makes for a   
   big doghouse to bump into right about crotch height (depending on the   
   knee height).  The extra heavy stepper is shorter than the servo, and if   
   I write the end program macro and tool change macros to move the saddle   
   all the way out from the column it will be mostly under the table top   
   enclosure anyway. I also no longer need to stand in front of the machine   
   doing manual work with the MPG since I have a half decent manual machine   
   now.   
      
   Both the X & Y axis will be getting new ball screws and new fixed end   
   bearings.  I found a vendor with some decent quality (claimed) metric   
   ball screws about the right size and better backlash than Hurco claimed   
   for that machine in the manual.  I'll have to pick a micro step count   
   that comes out to a nice even steps per inch, but I've done that with   
   metric ball screws before.   
      
   ** Hurco claimed .003 or better in the manual I have.  When I first got   
   it running I was getting much better than .001 not counting flex.  For   
   aluminum there really was no significant flex.  In steel it would run   
   better than .003 including flex all day, and of course I could program   
   multiple cleanup passes with an "MO" stop to measure and hit the stop   
   button or hit resume.  I have to add that was total flex.  I didn't   
   realize back then how much of that was the tool itself.   
      
   The X axis will be configured they same as the Y, but with one of the   
   regularly massive NEMA 34 steppers.  I may need to make a new doghouse,   
   or I may be able to get away with just cutting that one shorter.   
      
   I don't know about the Z.  Currently the backlash is good, and most of   
   that is taken up by the weight of the quill anyway.  I am thinking if I   
   eliminate the belt drive on it as well I might be able to use that   
   recovered power lost in the belt for a little more acceleration.  If I   
   go direct drive I will have to make a new head cover for the top since   
   the motor would be sticking up.   
      
   Ideally I would love to see reliable 30iss (or better) and 250-300ipm.   
   Yeah I ran that much with the original GeckoDrives and they kept frying   
   even though Gecko swore they could take it.  I kept turning down the   
   current, rapids, and acceleration, and the Geckos still kept frying.   
   Later I ran the servos with an ammeter connected while adjusting the   
   gibbs, and they never should have been dying.  The Geckos just suck.   
   The Dugong 160-35s have been pretty good.  Acceleration initially was   
   insane as was rapid speed, but once I started tuning them, and reducing   
   following error they were little better than the Geckos... except they   
   didn't fry if you looked at them cross eyed like the Gecko drives.   
      
   I really like the number of error outputs on the drives.  I can setup a   
   diagnostic bank to show me what error "exactly" is happening instead of   
   having to guess or go plugin the laptop with servo tuning software and   
   hope I can duplicate it.   
      
   Probably I'll go back to my old breakout board too.  All the inputs are   
   settable as high or low trigger.  Not so with the current BOB.  I had to   
   use low current trigger relays for some of the senors to swap the high   
   and low.  Blech.  I'll keep the ethernet motion controller instead of   
   going back to the USB one.  The BOB plugins for them are the same on   
   both boards.  The current BOB also didn't tune as cleanly for 0-10 RPM   
   output, and forward reverse triggering.  The old one was dead nuts at   
   every speed I ever checked it from 96RPM (3hz) to 3600 (120hz) after the   
   initial setup.   
      
   It's been a while.  I'm probably going to have to relearn a lot of the   
   setup.   
      
   I'll probably be getting rid of the old Mitsubishi VFD for spindle motor   
   control.  It tops out at 120hz.  I've got a little turret lathe that   
   might go on.  I have since learned that Hurco used to do an upgrade to   
   these machines to bump them to 6000 rpm (200hz) without changing the   
   spindles or upgrading the bearings.  I put new bearings in this spindle   
   a while back.  Not that many hours of run time though.  After break-in   
   they run quiet without getting hot, so I guess I must have done it   
   right.  I also have another set of new old stock original bearings in   
   the control cabinet.  If I bump this spindle to 6000 rpm any program I   
   already have for the Tormach (5120 rpm) will run on this machine.  I   
   already have a slightly larger spindle on hand I used briefly for a   
   companion spindle that will run up to 400hz.  I've programmed these VFDs   
   before, so setting it to top at 200hz should be pretty easy.   
      
   It seems Mach 3 does not support rigid tapping.  I had hoped to pick a   
   good RPM and use the Hurco for tension compression tapping (pseudo rigid   
   tapping).  An upgrade to Mach 4 or a switch to LinuxCNC may be in order   
   down the road.  LinuxCNC doesn't run my motion controller so that would   
   mean another BOB and motion control swap, but LinuxCNC (core of Tormach   
   Pathpilot) is really clean and has a great trajectory planner.  I have   
   grown to really like the PathPilot software running my Tormach.  The   
   thing is I have never successfully setup LinuxCNC before.  I tried a   
   couple times, but went back to Mach 3 because I just knew how to set it   
   up.  Oh.  I can't run any Tormach Code file after all.  I use tension   
   compression tapping on it all the time.  Maybe copy the Tormach style   
   library to a Hurco library and change all the TC styles to   
      
   [continued in next message]   
      
   --- SoupGate-Win32 v1.05   
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